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Preventing Detonation
We knew going into this project that putting boost on a 10.5:1 compression engine is an easy recipe for a blown head gasket, or worse yet a damaged motor. We had to take the proper precautions to prevent detonation and a lean condition. This meant ensuring adequate fuel delivery and quality, as well as controlling timing. We tackled both of these before pushing the motor hard on the dyno.

In naturally aspirated form we ran the 331 with 14 degrees initial and about 36° total (22° from the centrifugal advance mechanism.) For boost we dialed back initial to just 10°. However this yielded a total of 32° and we wanted to start tuning with no more than 24°. We adjusted the advance slot in the MSD Pro-Billet distributor by increasing the diameter of the stop bushing, however we could not get below 30° total. We called MSD for some advice. They turned us to their Boost Timing Master ignition system (see side bar.) The 6BTM will take out 1, 2 or 3 degrees of timing per psi of boost, up to 15 degrees maximum. If the Vortech S-trim puts out 6 psi we should see 6, 12, or 15 degrees reduced from total advance. In our case, with total at 32°, we can get timing to a conservative 20 degrees.

The next step in preventing detonation would be to raise the octane level of the fuel. The high static compression combined with the high dynamic
compression and temperature increase from the boost pressure is likely to result in spontaneous combustion due to pre-ignition or detonation. If combustion occurs when the piston is not in the top dead center position severe engine damage will result. With 91 octane in the tank we were detecting detonation at just mid-throttle in 4th gear. This was a sure sign we'd be in for trouble at wide open throttle on the chassis dyno. As a result we dropped in a few gallons of 110 leaded race gasoline. Blended with the remaining 91 in the tank we figure we were at around 105 octane.

Boosted Dyno Results
We headed back up to Advanced Dyno and paid for their ten pull tuning session, again using a wide-band oxygen sensor to monitor air-fuel ratio. We anticipated that proper tuning would take more than a day and planned to make several runs today to check over the basics such as proper fuel pressure, maximum boost pressure, and to baseline the air-fuel curve. We made the first pull with 76/79 jets in the same 750 double pumper we'd been running naturally aspirated.

Video
The air-fuel ratio on the first curve started going dangerously lean almost immediately. At 5000 rpm the curve went into the 16's (green plot below), and the dyno operator frantically motioned the kill engine sign. It was no surprise that horsepower was even less than in naturally-aspirated form. A lack of fuel at best will rob power, and at worst will rob you of an engine. Of lesser concern but nonetheless eyebrow raising, was our maximum boost was registering at only 4 psi on the playback gauge. This may not have been a bad thing considering any more boost would have increased the chance of engine damage due to the lean condition.

The question was why was the carburetor was going so lean. The dyno gurus again seemed to have an answer. They suspected the power valve channel restriction (PVCR) was not able to supply the amount of fuel the engine needed. Power valves are generally in the

Power Valve Channel Restriction (PVCR) diameter may have limited our engine performance.
primary metering block and rated to open at specific engine vacuum levels. This enables a smaller jet size for fuel-efficient part throttle driving, while enabling enrichment under high-load and wide open throttle conditions. The orifice size of the jet plus the orifice size of the PVCR determines the amount of total fuel which can enter the primary circuit. In a blow-through application the diameter of the PVCR often needs to be increased to flow more fuel. As a temporary measure, and test of theory, we removed the power valve and placed a power valve plug in its place. We jetted up to 80's in the primary and 84's in the secondary to compensate for the fuel we would not be getting via the PVCR. This is a common tactic for race cars but results in poor part throttle fuel economy and performance for street cars. The engine responded to the additional fuel and while still dangerously lean at 14:1, power was up to 416 horsepower and 410 lb.ft. of torque.

Dynojet Results: Supercharged, 331cid
  Peak Horsepower Peak Torque (lb.ft)
Initial 351.1 @ 6000rpm 400.2 @ 4000rpm
Best 424.6 @ 6000rpm 406.4 @ 5100rpm

Last Pull
With all systems checking out ok and no detonation detected we jetted up the secondaries to 91 in attempts to get the air-fuel ratio into the rich side. The third pull continued the trend of increasing power while AF ratio

Advanced Dyno's H.H.Bennet sports the usual mile wide smile after seeing the power numbers resulting from his tuning advice.
was now at a steady 13.5 - still lean but getting closer. We expected to see a much larger change in AF ratio with the seven-size increase in secondary jets. The fact that we saw only a net change of 0.5 was an indicator that the carburetor was at its' limits for supporting this engine. This is not to say that the 750 cfm rating is the limiting factor, but rather the carbs ability to meter the proper amount of fuel for the amount of air being consumed by the supercharged engine. This didn't come as a surprise and in fact prior to this dyno session we were already in discussions with a leading carb tuner for a blowthrough specific carburetor.

The red plot in the chart above shows the third and final pull for the day, with peak horsepower at 424 and torque at 406 lb.ft.
We still are seeing only 4 psi of boost on the guage. The S-trim blower is rated to produce between 6-8 psi on a 302 displacement engine. While 4 psi seems low it may be due to the increased displacement of our stroker plus the efficiency of the engine. The bottom line is not boost but power numbers. Currently we're only netting 55 horsepower and 65 lb.ft of torque above our naturally aspirated results, but we're nowhere near being tuned. Watch for our final article in this series with results from round two.
 
 








Turn Back Time

We're using MSD's Boost Timing Master (6BTM) to retard timing as boost pressure builds. A dash mounted dial enables 0-3 degrees of retard per psi of boost. This will enable us to run 10-12 degrees initial and as little as 26 total to ward off detonation.
The 6BTM box is identical to the famed 6AL ignition, save for the 1/8" vacuum nipple for boost reference. Installation is equally as easy with the added step of locating the timing dial within drivers reach.
Source:
MSD Ignition

Autotronic Controls Corporation
12120 Esther Lama, Suite 114
El Paso, Texas 79936
www.msdigniton.com

 
 
 

 

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